I made a new Z-axis motor coupler, as I suspect the old one was slightly off-center & causing wobbles to show in printed parts. The new one seems better, but I still have a little bit of wobble from a still undetermined source.
Here are a few recent prints. I recently started using the “Dimension” module within Skeinforge to retract the feed-stock between moves, and it’s really helped reduce the “stringies” that’d happen between parts.
These rings printed fine, but a few lost their grip right as the print finished.